It looks like you're using an Ad Blocker.
Please white-list or disable AboveTopSecret.com in your ad-blocking tool.
Thank you.
Some features of ATS will be disabled while you continue to use an ad-blocker.
Transcripts derived from the cockpit voice recorder suggest the crew, speaking in a mixture of English and Mandarin, failed to grasp the nature of the situation. There were three people in the cockpit: two captains and a first officer in the jump seat as an observer pilot.
“Had the crew prioritised their actions to stabilise the aircraft flight path, correctly identify the propulsion malfunction… then take actions in accordance with procedure of engine number 2 flame-out at take-off, the occurrence could have been prevented,” says the report.
“Flight crew coordination, communication, and threat and error management were less than effective, and compromised the safety of the flight.”
Besides crew error, investigations also identified other contributing factors such as the airline’s flight operations processes and regulatory oversight of TransAsia by the Civil Aeronautics Administration.
The report adds that the intermittent signal discontinuity in the right engine’s AFU may have caused the ATPCS to not be armed during take-off roll, or was activated during the initial climb, which resulted in a complete ATPCS sequence including autofeathering. Evidence indicated that the discontinuity was likely caused by compromised soldering joints inside the AFU.
but you have to finance $250,000 to do it.
originally posted by: GBP/JPY
really poor flying....from two pros....the third couldn't feel the rudder pedals.....in a twin, when one engine has trouble and one side pulls, the pedal you step on is the side with the turbine working...then add wings level...